TriMotoRevival is about my experiences reviving Triumph motorcycles made in Hinckley the 1990's. These are the so-called 'T300' models, using the Hinckley factory codes for machines of this era. I started it to document the process of renovating my Lancaster Red 1991 Triumph Trophy 1200, VIN #544. Since I completed the rebuild on #544, I've added written about trips, other early Hinckley bikes, and work on my Racing Yellow 1994 Triumph Daytona 900. I hope you enjoy what you find here.
Friday, May 24, 2013
New PVL twin outlet coils
I was convinced it wasn't a fueling problem, after all the work I'd done on the tank, and the carbs, and the fuel pipes ... ! Starting from cold was OK - firing after maybe four or five spins of the engine on the starter.That's why I thought it was time to revisit the ignition system to look for an explanation. I'd previously had a problem with my Daytona cutting out when warm and that was due to electrical breakdown of the ignition pickup coil when the engine was hot. It had always started perfectly from cold and, after cutting out, would re-start from cold. In that case though, it was total failure with the engine stopping completely while riding at normal speeds.
With my Trophy, it was different because it would run reasonably well at normal speeds though would cough occasionally accelerating from low revs. I'd read about similar problems on some internet forums. They pointed to failing ignition coils as the potential cause.
On my Trophy, these are a pair of twin-outlet resin-encapsulated units manufactured by PVL in Germany. The PVL coils on my bike were the originals. I know because PVL stamp the production date just above the low-tension connections on their coils. Mine read 0491 - April 1991.
So that means they are 22 years and one month old. That's old enough to justify retiring them. The coils I bought from Sprint were marked 1112 and 0313 - November 2012 and March 2013. I was somehow amazed to see that their construction appeared to be identical in every way to the originals - same cases, same potting, same terminals.The only difference is the white print on the body, with the code 356 100. The PVL website lists that code as "High performance double Ignition Coil 2/4-cylinder Triumph, BMW", 1.1Ohm primary winding, secondary 7,66kOhm. My old analogue multimeter sort of agreed with this, given that the needle waves about quite a lot without ever seeming to settle. I noticed that the secondary windings on the old coils were reading about 10kOhm - higher than the new ones anyway. This measurement doesn't mean much though because the bike was cold when I measured the resistances and the problem only surfaces when hot.
I smiled to see 'Made in W Germany' still moulded into the plastic cases. It was hard to believe so much time could have passed with absolutely no evidence of design change. Of course, changes could be hidden inside.
I've been for one ten-mile run with the new coils so far and already the difference is noticeable. No more coughing on the throttle at low revs. Whilst idling on its centre stand after the ride, I got the bike hot enough or the fan to cut in. Whereas it would have been stumbling badly yesterday, there was just a hit of lumpiness. I was able to turn the idle speed right down to an indicated 500 rpm without the bike stalling. I must have left it running like that for a minute just to see before turning it back up to its regular 1000 rpm idle speed.
Friday, November 2, 2012
A Trip to Trevor

He was impressed with the quietness of the motor compared with others of its ilk. He told me the early die-cast cases (with access hatch for sprag and alternator drive gears) are noticeably quieter than the later Cosworth pressure sandcast cases. I forgot to say that the 1991 bikes have foam-lined fairing panels too, dampening the sound further. And the result. Well, was it in doubt? I think it met with his approval.

The bike had run beautifully all the way there. Irritatingly, I had more fueling problems on the way home. Maybe the bike was sad to have had to leave the cosseting world of Sprint. But seriously, I think I've got four issues to deal with, two of which are probably self-inflicted. 1/ The loose sheets of liner are wrapping themselves around the fuel tap's integral filter 2/ the fuel tap prime position isn't passing any fuel, 3/ the angle of the extended fuel pipes and filters I fitted seems to be causing at least one hose to fold. 4/ The extended pipes are also putting pressure on the vacuum pipe to the rear of the fuel tap. So I shall address all these issues before taking her out on the road again.
Thursday, July 5, 2012
Pitted fork repair, Sprint Manufacturing 20% uprated springs, and front wheel refit
I decided to try comparing the spring rates. No pics I'm afraid but I did this by placing an old kitchen scales upside down on each of the springs and then compressing them for 1cm. I was surprised to find that the Sprint springs were about 6kg per cm whereas the ones I removed were 6.5kg per cm. In other words, harder. So maybe they aren't the originals. However, the Sprint springs have two pitches whereas the springs I removed were evenly wound along their entire length. The manual indicates that the originals should be twin rate. I decided I'd try to see what the rate of the Sprint springs are when the close-wound section binds. I did this by clamping the spring in my workmate just above the close-wound section and repeating the scales trick. This time, it showed a rate of 7kg per cm, so about 17% stiffer by my imprecise measurements - close enough to Sprint's claim for me to believe all is in order.
Forks reassembled, I decided to fit a pair of stone guards. The clamp just above the dust seals. Hopefully, they'll help to keep the Chemical Metal repair functional for a little while at least.
I found that the front wheel axel was rusted internally. There is a plastic bung on the left hand end that had been damaged, allowing water ingress. So I cleaned it up with a drill and thin wire brush, primed and painted it before coating the bung in waxoil and refitting. I also gave the front axel nut a birthday.
I like polishing. The fork top nuts and speedo gearbox gave me a chance to break out the Solvol and bling it up :-)
Plenty of LM grease on the axel and the wheel is back in place. The axel can be held still with a tommy bar through the left hand end whilst the nut is pinched up. There was zero clearance between the fork legs and the wheel spacer (left) and speedo gearbox (right) so it was a performance getting the wheel in place. I managed it in the end by slackening the fork clamp bolts in the lower yoke and slightly twisting the sliders.
For torquing the axel up, it is necessary to tighten two clamp bolts in the left-hand fork leg so the axel doesn't rotate. The two clamp bolts in the right-hand leg can then be torqued too.
Handlebars and clocks loose fitted, starting to look like a bike again.